EFTA00597054.pdf
PDF Source (No Download)
Extracted Text (OCR)
Gulfstream
INVOICE
A NNN
OVNAMICA
COMPANY
7 Char Drive - Westfield. Massachusetts 01085-1493
Part/Model #:
AC Serial No/Tail No.:
Mail Remittance To:
Gulfstream Aerospace Corporation
•. Box 730349
Dallas, Texas 75373-0349
Overnight Remittance To:
Gulfstream Aerospace Corporation (Box N 730349)
do JP Morgan Chase Bank. NA
ATTN: Dallas National Wholesale Lockbox TX1-0029
14800 Frye Road
Ft. Worth, TX 76155
Wire Remittance To:
Gulfstream Aerospace Corporation
JP Morgan Chase Bank, NA
Chicago, IL 60670
Account No. 10-15825
Fedwire Routing No. (ABA) 021 000 021
S.W.I.F.T. CHASUS33
ACH Credit Routing No. (ABA)071 000 013
Bill To: HYPERION AIR, INC.
3800 SOUTHERN BLVD
SUITE 204
WEST PALM BEACH, Florida 33406
United States
Title: HYPERION AIR, INC.
Invoice Number:
Invoice Date:
Customer ID:
Number:
Repair Station:
In Date:
Out Date:
Payment Type:
Payment Terms:
6916001251
41812016
CH200
CRS LECR039G
03/05/2016
03/25/2016
Net 30-Open terms
INVOICE SUMMARY FOR WORK ORDER NUMBER:
Time & Materials
SC13577
Flat Rate
Total
Labor USD:
523,752.08
50.00
523,752.08
Pans USD:
510,546.36
50.00
510,546.36
Services USD:
513,050.98
50.00
513.050.98
Detail Subtotal USD:
$47,349.42
50.00
S47.349.42
Subtotal USD:
$47,349.42
Funds on Deposit USD:
50.00
Total USD:
SCHEDULED MAINTENANCE
FAR PART 91
LARRY VISOSKI 917-868-6145
N2I2JE
RE: PROPOSAL# 7024273 1201 (GAC1015-2422-GIV-)085-R01)
7024691 R00 (GAC0216-4691-GIV-)085-120D)
HAPP # 4400-529-21
$47,349.42
For detail description of the work complied with see the Work Order Detail report.
Westfield_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rpt
Page 1 of 14
Printed: 4(912016 4:26:50AM
LS MO
EFTA00597054
Bill To: IIYPERION AIR, INC.
WO #: SCI3577
Invoice Number: 6916001251
Item: 6
AVIONICS
Team Manager:
Charles Helwig
Customer Coordinator:
Vinny Cicala
Pan/Model #:
AC Serial No./Tail No.:
TSN/TSO:
CSN/CSO:
Aircraft Time:
Discrepancy: 6.1
CUSTOMER REPORTS #1 TRANSPONDER LOOSES ATC ALTITUDE READ OUT AFTER ONE HOUR.
Resolution: UNSEATED ATC NO.1 PN: 622-9210-409 SN: 2376. PERFORMED VISUAL INSPECTION OF BOTII THE RACK
AND COMPONENT INSURING NO BENT OR PUSH PINS ARE PRESENT. CLEANED CONTACTS AND
RESEATED ATC NO.1 PN: 622-9210-409 SN: 2376. DISCONNECTED INTERCONNECT FOR ATC NO.1 AND
FOUND MALE PINS S AND T TO BE BENT AND MAKING LIMITED CONTACT WITH FEMALE PINS. WORK
PERFORMED IN ACCORDANCE WITH WIRING DIAGRAM 1159SB41481, GIV AMM 34-02-04 AND GIV WIRING
DIAGRAM 34-55-00. REMOVED ATC NO.2 P/N:622-9210-409 SIN: 1G8hil. UNSECURED ATC RACKS TO
FACILITATE MAINTENANCE. REPLACED ATC NO.1 DISCONNECT CONNECTORS P/N: MS3120F22-55P SN:
UNK AND P/N: M53126F22-55S SN: UNK, RECEIVED P/N: MS3120F22-55P FROM ELECTRO ENTERPRISE
REFERENCE CERTIFICATE OF CONFORMANCE ON PACKSLIP NO: 1779462 DATED 03/14/2016. RECEIVED
P/N:MS3126F22-55S FROM ELECTRO ENTERPRISES REFERENCE CERTIFICATE OF CONFORMANCE WITH
INVOICE NO: 1156087 DATED 05/25/11. PERFORMED WIRING RING OUT CHECK OF ATC NO.1
TRANSPONDER LAW WESTERN COMMANDER WIRING DWG NO:08069197, FOUND GOOD. REINSTALLED
SERVICEABLE ATC NO.1 PN: 622-9210-409 SN: 2376 AND SERVICEABLE ATC NO.2 P/N:622-9210-409 SIN: 1G88/1
AND PERFORMED ATC FUNCTIONAL CHECKS IN ACCORDANCE WITII GIV AMM 34-02-04. NOTED NO
FURTIIER ISSUES AT TIIIS TIME. SEE STEPS FOR DETAILS.
Billing Method
Hours
Rate
Total
Labor USD:
Time and Material
ST
39.91 ®
$132.00
$5,268.12
Parts USD:
Time and Material
$211.08
Total USD:
$5,479.20
Parts:
Ref. No.
Pan number
Description
Quantity
Sell price USD
Extended USD
6.1 #1
hIS3120F22-55P
CONNECTOR
1
$95.68
595.68
6.1 #2
hIS3126F22-55S
CONNECTOR
1
$8536
585.36
6.1 #3
686DM3
SLEEVE. BRAIDED 1/2 BLACK
2
53.92
$7.84
EXPANDO
6.1 #4
SPT.50
SPIRAL WRAP TEFLON 1/2"
2
53.30
56.60
NATURAL
6.1 #5
TY25M
TYRAP, WHITE
10
50.78
57.80
6.1 #6
TY242M
TIE, CABLE; NYLON 8.19 IN.; 0.14
10
50.78
57.80
IN.; 30 LB. TENSILE STRENGTH
For detail description of the work complied with see the Work Order Detail report.
Westfield_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rpt
Page 2 of 14
Printed: 49/2016 4:26:50AM
LS MO
EFTA00597055
Bill To: HYPERION AIR, INC.
WO #: SCI3577
Invoice Number: 6916001251
Step: 6.1.1
Completed
APPLIED POWER TO AIRCRAFT. MONITORED ALTITUDE REPORTING ON
BOTH ATC TRANSPONDERS USING ATC 600 TEST SET FOUND GOOD. LET IT
RUN FOR A LONG TIME, WHILE PERFORMING ASCB BUS SWEEP (REF.
SQUAWK 63), FOUND GOOD AT THIS TIME. WORK WAS DONE REFERENCE
GIV A.M. 34-02-04.
Step: 6.1.2
Completed
UNSEATED ATC NO.1 PN: 622-9210-409 SN: 2376. PERFORMED VISUAL
INSPECTION OF BOTH RACK AND COMPONENT INSURING NO BENT OR
PUSH PINS ARE PRESENT. CLEANED CONTACTORS AND RESEATED ATC
NO.1 PN: 622-9210-409 SN: 2376. GAINED ACCESS TO AND DISCONNECTED
INTERCONNECT FOR ATC NO.1 AND FOUND MALE PINS S AND T TO BE
BENT AND MAKING LIMITED CONTACT WITH FEMALE PINS.
STRAIGHTENED PINS AND RECONNECTED DISCONNECT. APPLIED POWER
TO AIRCRAFT AND PERFORMED MULTIPLE CHECKS OF ATC SYSTEM
USING IF'R 6000. NOTED NO OCCURENCES OF TRANSPONDER FAILING TO
REPORT ALTITUDE. ALL WORK PERFORMED IN ACCORDANCE WITH GIV
AMM 34-02-04 AND WIRING DIAGRAM I159:O341481.
Step: 6.13
Completed
STEP ENTERED IN ERROR
Step: 6.1.4
Completed
CONDUCTED RESEARCH TO FIND PART NUMBER FOR ATC TRANSPONDER
INTERCONNECT CANNON PLUG PART NO. PART NUMBER FOR
RECEPTACLE IS MS3120F22-55P PART NUMBER FOR PLUG IS
MS3126F122-555. REFERENCE WESTERN COMMANDER DRAWING NO.
08069197. TITLED NO. 1 TRANSPONDER (MOD) NO REV, DATED 5/12/89. THIS
CONNECTOR CONTAINS VARIOUS 429 DATA INPUTS/OUTPUTS FOR
CONTROL AND TUNING, SUPPRESSION SIGNALS AND TCAS INTERFACE.
AND POWER. ALL WORK PERFORMED IN ACCORDANCE WITH WESTERN
COMMANDER DRAWING NO. 08069197, TITLED NO. I TRANSPONDER (MOD)
NO REV, DATED 5/12189
Step: 6.1.5
Completed
REMOVED ATC NO.2 P1N:622-9210-409 S/N: 1G8M. UNSECURED ATC RACKS
TO FASCILITATE MAINTENANCE. REMOVED ATC NO.1 DISCONNECT
CONNECTORS P/N: MS3120F22-55P SN: UNK AND P/N: MS3126F22-55S SN: UNK.
INSTALLED NEW CONNECTORS P/N: MS3120F22-55P SN: UNK AND P/N:
MS3126F22-555 SN: UNK. RECEIVED P/N: MS3120F22-55P FROM ELECTRO
ENTERPRISE REFERENCE CERTIFICATE OF CONFORMANCE ON PACKSLIP
NO: 1779462 DATED 03/14/2016. RECEIVED P/N:MS3126F22-55S FROM
ELECTRO ENTERPRISES REFERENCE CERTIFICATE OF CONFORMANCE
WITH INVOICE NO: 1156087 DATED 05/25/II. ALL WORK PERFORMED IN
ACCORDANCE WITH WIRING DIAGRAM 1159SB41481.GIV AMM 34-02-04 AND
GIV WIRING DIAGRAM 34-55-00.
Step: 6.1.6
Completed
PERFORMED WIRING RING OUT CHECK OF ATC NO.1 TRANSPONDER IAW
WESTERN COMMANDER WIRING DWG NO:08069197 FOUND GOOD.
Discrepancy: 6.2
CUSTOMER REQUEST TO EXCHANGE THE #2 COM STICKY COM SELECTOR TO CHANGE
FREQUENCY.
Resolution: APPLIED POWER AIRCRAFT, CHECKED OPERATION OF NO.2 RADIO TUNING UNIT (RTU), SQUAWK
CONFIRMED, FOUND LINE SELECT KEY (1R) IS INTERMITTENT (STICKY) TO CHANGE FREQUENCY.
REMOVED RTU NO:2 P/N:822-0836-035 SIN: 267 FOR REPAIR. RECEIVED OK TO INSTALL AND INSTALLED
REPAIRED RTU NO:2 P/N:822-0836-035 SIN: 267 IN ACCORDANCE WITH GIV CMP 232336. RECEIVED UNIT
FROM ROCKWELL COLLINS REFERENCE 8130-3 WITH FORM TRACKING NO: 105121875 WORK ORDER:
WEP016-01211 CERT: ED7Y210Y DATED 16MAR2016. PERFORMED VIIF COMMUNICATIONS SYSTEM -
OPERATIONAL CHECK IN ACCORDANCE WITH GIV AMM 23-01-00,MARKER BEACON SYSTEM -
OPERATIONAL CHECK IN ACCORDANCE WITH GIV AMM 34-02-02, NAVIGATION / DISTANCE MEASURING
EQUIPMENT SYSTEMS - OPERATIONAL CHECK IN ACCORDANCE WITH GIV AMM 34-02-02, AUTOMATIC
DIRECTION FINDING SYSTEM - OPERATIONAL CHECK IN ACCORDANCE WITH GIV AMM 34-02-03.
Billing Method
Hours
Rate
Total
Labor USD:
Time and Material
ST
8.23
S132.00
$1,08636
Services USD:
Time and Material
S8,572.23
Total USD:
49,658.59
Services:
Ref. No.
Description
Quantity
Sell Price USD
Extended USD
For detail description of the work complied with see the Work Order Detail report.
Westfield_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
Printed: 4(912016 4:26:50AM
Orderinvoice.rpt
Page 3 of 14
LS MO
EFTA00597056
Bill To: HYPERION AIR, INC.
Services:
WO #: SCI3577
Invoice Number: 6916001251
Ref. No.
Description
Quantity
Sell Price USD
Extended USD
6.2 #2
GAC REPAIRS
1.00
58,57223
58,572.23
Part Ref: 822-0836-035 RTU-4200 (RADIO TUNING UNIT)
62#1
GAC REPAIRS
1.00
50.00
S0.00
Step: 6.2.1
Completed
APPLIED POWER AIRCRAFT, CHECKED OPERATION OF NO.2 RADIO
TUNING UNIT (RTU), SQUAWK CONFIRMED. FOUND LINE SELECT KEY
(1R) IS INTERMITTENT (STICKY) TO CHANGE FREQUENCY.
NEED TO REPLACED OR SEND FOR REPAIR RTU NO.2.
Discrepancy: 6.3
CUSTOMER REPORTS THE #2 IIF RADIO WILL NOT TUNE ("CP" AND "RT" LIGHT ILLUMINATES).
Resolution: GAINED ACCESS ON TAIL COMPARTMENT, VISUALLY INSPECTED THE IIF COUPLERS AND IIF
TRANSCEIVERS, FOUND THE RF COAX CONNECTOR ON IIF COUPLER NO.2 IS LOOSE. SECURED COAX
CONNECTOR ON IIF COUPLER NO.2.
PERFORMED HIGH FREQUENCY COMMUNICATION SYSTEMS NO. 1 AND NO.2 - OPERATIONAL TEST,
CHECKED GOOD ON BOTH SYTEM. RF RADIO CHECKS CONDUCTED WITH NY RADIO WITH TXJRX
QUALITY 4X4. WORK DONE IAW GULFSTREAM GIV MM ATA 23-03-00.
Billing Method
Hours
Rate
Total
Labor USD:
Time and Material
ST
4.48
®
$132.00
559136
Total USD:
5591.36
Step: 6.3.1
Step: 6.3.2
Completed
APPLIED POWER TO AIRCRAFT, PERFORMED HF NO. I AND NO.2 SYSTEM
OPERATIONAL TEST, FOUND NO.2 HF SYSTEM WITH "CP" LIGHT
ILLUMINATED AND WITH FAULT 08. ASKED CUSTOMER ABOUT THE HF
SQUAWK DUE TO HF SYSTEM NO. I IS THE ONE FAILED ON THE ITEM. PER
CUSTOMER. HE IS NOT SURE WHAT SYSTEM IS FAILING. GAIN ACCESS ON
TAIL COMPARTMENT, VISUALLY INSPECTED THE HF COUPLERS AND HF
TRANSCEIVERS, FOUND THE RF COAX CONNECTOR ON HF COUPLER NO.2
IS LOOSE. SECURED COAX CONNECTOR ON HF COUPLER NO.2.
PERFORMED HIGH FREQUENCY COMMUNICATION SYSTEMS NO. I AND
NO. 2 - OPERATIONAL TEST, CHECKED GOOD ON BOTH SYTEM. WORK
DONE IAW GULFSTREAM GIV MM ATA 23-03-00.
Completed
USING 0-IS PSIG PRESSURE GAUGE, CHECKED THE PRESSURE IN BOTH NO.
1 AND NO.2 HF COUPLERS. NO. 1 COUPLER WAS AT 7 PSI AND NO. 2
COUPLER WAS AT APPX. 6.75 PSI. BOTH OF THESE READINGS ARE WITHIN
ALLOWABLE PRESSURES AS PER GIV
23-03-00, HIGH FREQUENCY
COMMUNICATION COUPLER - SERVICING.
Discrepancy: 6.4
CUSTOMER REPORTS THE FMS SELECTOR SWITCH NEEDS TO BE CHANGED (1/2 FMS SELECTOR
ON CENTER PEDESTAL).
Resolution: CONFIRMED CENTER FMS SELECTOR WILL ONLY BRIEFLY ILLUMINATE 1/2 FMS. REMOVED AND
CAPSULE AND REMOVED 4 EA. DEFECTIVE LAMPS P/N OL-3335, NO SERIAL NOS. REPLACED WITH 4 EA
NEW LAMPS P/N: 01.-3335 FROM GAC WESTFIELD STOCK. PERFORMED OPERATIONAL CHECK OF
SWITCHES IN ACCORDANCE WITH GIV AMM 33-01-00 ANNUNCIATOR LIGHT-OPERATIONAL TEST, WITH
NO DISCREPANCIES.
Labor USD:
Pans USD:
Total USD:
Billing Method
Hours
Rate
Total
Time and Material
Time and Material
ST
6.71 ®
5132.00
5885.72
5360.50
41,246.22
For detail description of the work complied with see the Work Order Detail report.
Westfield_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rpt
Page 4 of 14
Printed: 49/2016 4:26:50AM
LS MO
EFTA00597057
Bill To: HYPERION AIR, INC.
Parts:
WO #: SC13577
Invoice Number: 6916001251
Ref. No.
Part number
Description
Quantity
Sell price USD
Extended USD
6.4 #1
OL3335
LAMP
6.1#2
99-212
SWITCH
Step: 6.4.1
Step: 6.4.2
4
$5.15
$20.60
$339.90
$339.90
Completed
GAINED ACCES TO THE FMS SELECTOR SWITCH (1/2 FMS) ON PEDESTAL.
REMOVED DEFECTIVE SWITCH (1/2 FMS) P/N: 99-212 FROM ASSEMBLY.
RECEIVED OK TO INSTALL AND INSTALLED A NEW SWITCH P/N: 99-212
THAT WAS RECEIVED FROM GAC-SAVANNAH WITH SHIPMENT NO.:
SASH316-34302, ENTERPRISE TRANSFER NO.: 000663760, DATED 03/08/2016 TO
THE (1/2 FMS) SWITCH POSITION ON ASSEMBLY. SECURED SWITCH
ASSEMBLY TO PEDESTAL WORK WAS DONE WITH REFERENCE TO THE
JET CENTER DRAWING NO. 08069100, TITLED NO. 3 FMS, DATED 3-11-88.
Completed
PERFORMED OPERATIONAL CHECK IN ACCORDANCE WITH GIV AMM
33-01-00 ANNUNCIATOR LIGHTS - OPERATIONAL TEST, WITH NO
DISCREPANCIES.
Discrepancy: 6.5
CUSTOMER REQUESTS ASCB SWEEP
Resolution: PERFORMED ASCB BUS SWEEP IAW GIV
31-02-00. FOUND THAT THERE WERE NUMEROUS BUS
COUPLER CONNECTIONS THAT REQUIRED CLEANING (NOTICED SIGNAL FLUCTUATION ON
OSCILLOSCOPE). CLEANED BUS COUPLER CONNECTIONS AS REQUIRED AND SECURED ALL
CONNECTIONS. PERFORMED OPS CIIECK AND FINAL ASCB BUS SWEEP IN ACCORDANCE WITH GIV
AMM 31-02-00 AVIONICS STANDARD COMMUNICATION BUS - FAULT ISOLATION WITH NO
DISCREPANCIES.
Billing Method
Hours
Rate
Total
Labor USD:
Time and Material
ST
13.00 ®
$132.00
31,716.00
Total USD:
41,716.00
Step: 6.5.1
Completed
PERFORMED ASCB BUS SWEEP 1AW GIV MM. 31-02-00. FOUND THAT
THERE WERE NUMEROUS BUS COUPLER CONNECTIONS THAT REQUIRED
CLEANING (NOTICED SIGNAL FLUCTUATION ON OSCILLOSCOPE).
CLEANED BUS COUPLER CONNECTIONS AS REQUIRED AND SECURED ALL
CONNECTIONS. CHECKED ASCB BUS CHANNELS A AND B, FOUND GOOD AT
THIS TIME.
Discrepancy: 6.7
WHILE PERFORMING SPZ-8000 CND MAINTENANCE TEST NOTICED THAT TFIE LEFT FUEL LOW
LEVEL INDICATION STAYS WHITE IN ECIAS AND NO LIGHT ON STANDBY FUEL INDICATION WITH
ZERO FUEL ON WING.
Resolution: PERFORMED RESISTANCE CIIECK OF THE LEFT WING LOW LEVEL SENSOR AND FOUND TIIAT IT WAS
WITHIN LIMITS. WITH BOTH EICAS AND STANDBY FUEL QUANTITY INDICATOR SHOWING NO LOW
LEVEL WARNING, WITH ZERO FUEL ON TIIE LEFT WING. AT CONNECTOR 15A1P1, SWAPPED PINS C
(CLOSE DRY LEFT SIGNAL) WITH PIN D (CLOSE DRY RIGHT SIGNAL), AND THE PROBLEM FOLLOWED.
SWAPPED BOTII PINS BACK TO THEIR ORIGINAL POSITIONS. CONFIRMED BAD FUEL LOW LEVEL DUAL
CONTROL UNIT. REMOVED FUEL QUANTITY DUAL LOW LEVEL CONTROL UNIT PIN: 1159SCF215-33, SIN:
567 FROM THE AIRCRAFT. RECEIVED OK TO INSTALL AND INSTALLED A REPAIRED FUEL QUANTITY
DUAL LOW LEVEL CONTROL UNIT PIN: 1159SCF215-33,S/N: 690 THAT WAS RECEIVED FROM PARKER
HANNIFIN CORP., ELECTRONICS SYSTEMS DIV. WITII FAA 8130-3 FORM TRACKING NO.: 9E5210,
APPROVAL / CERTIFICATE NO.: FX1R156IC, DATED AUG/23/2010 TO THE AIRCRAFT. APPLIED POWER TO
TFIE AIRCRAFT AND FOUND THAT THE LEFT, RIGHT, AND TOTAL FUEL LEVEL INDICATION WAS AMBER
ON EICAS, ALSO THERE WAS LIGHT, (LEFT AND RIGHT) ON STANDBY FUEL INDICATOR. WORK WAS
DONE IAN' GIV CMP 284020, FUEL QUANTITY DUAL LOW LEVEL CONTROL UNIT - REMOVAL /
INSTALLATION. COMPLIED WITII GIV CMP 284029 FUEL LOW LEVEL WARNING SYSTEM - OPERAIONAL
TEST WITII NO DISCREPANCIES.
For detail description of the work complied with see the Work Order Detail report.
Westfield_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rpt
Page 5 of 14
Printed: 4(912016 4:26:50AM
LS MO
EFTA00597058
Bill To: HYPERION AIR, INC.
WO #: SCI3577
Invoice Number: 6916001251
Billing Method
Hours
Rate
Total
Labor USD:
Time and Material
ST
12.98
®
$132.00
31,713.36
Pans USD:
Time and Material
$4,737.00
Total USD:
$6,450.36
Pans:
Ref. No.
Pan number:
Description
Quantity
Sell price USD
Extended USD
6.7 #1
1159SCF215-33
CONTROL UNIT. FUEL, LOW LEVEL
1
$4,737.00
$4,737.00
Step: 6.7.1
Step: 6.7.2
Step: 6.7.3
Completed
PERFORMED RESISTANCE CHECK OF THE LEFT WING LOW LEVEL SENSOR
AND FOUND THAT IT WAS WITHIN LIMITS. WITH BOTH EICAS AND
STANDBY FUEL QUANTITY INDICATOR SHOWING NO LOW LEVEL
WARNING, WITH ZERO FUEL ON THE LEFT WING. AT CONNECTOR 15A1P1,
SWAPPED PINS C (CLOSE DRY LEFT SIGNAL) WITH PIN D (CLOSE. DRY
RIGHT SIGNAL), AND THE PROBLEM FOLLOWED. SWAPPED BOTH PINS
BACK TO THEIR ORIGINAL POSITIONS. CONFIRMED BAD FUEL LOW
LEVEL DUAL CONTROL UNIT. ALL WORK WAS DONE WITH REFERENCE
TO GIV
28-07-00.
Completed
REMOVED FUEL QUANTITY DUAL LOW LEVEL CONTROL UNIT PIN:
1159SCF215-33, S/N: 567 FROM THE AIRCRAFT. RECEIVED OK TO INSTALL
AND INSTALLED A REPAIRED FUEL QUANTITY DUAL LOW LEVEL
CONTROL UNIT PEN: 1159SCF215-33, S/N: 690 THAT WAS RECEIVED FROM
PARKER HANNIFIN CORP., ELECTRONICS SYSTEMS DIV. WITH FAA 8130-3
FORM TRACKING NO.: 9E5210. APPROVAL / CERTIFICATE NO.: F7C1R156K,
DATED AUG/23/2010 TO THE AIRCRAFT. APPLIED POWER TO THE
AIRCRAFT AND FOUND THAT THE LEFT, RIGHT, AND TOTAL FUEL LEVEL
INDICATION WAS AMBER ON EICAS, ALSO THERE WAS LIGHT, (LEFT AND
RIGHT) ON STANDBY FUEL INDICATOR. WORK WAS DONE TAW G1V CMP
284020, FUEL QUANTITY DUAL LOW LEVEL CONTROL UNIT - REMOVAL /
INSTALLATION.
Completed
COMPLIED WITH GIV CMP 284029 FUEL LOW LEVEL WARNING SYSTEM -
OPERAIONAL TEST WITH NO DISCREPANCIES.
Discrepancy: 6.8
DURING OW CMP GIV 541019 PYLON INTERNAL (LEFT) - INSPECTION FOUND PRECOOLER INLET
TEMPERATURE SENSOR CANNON PLUG TO HAVE BROKEN WIRE.
Resolution: REMOVED AND REPLACED CONNECTOR LEFT ENGINE PYLON TEMP SENSOR P/N 3153106F12S-35 NEW
FROM ELECTRO ENTERPRISES INC ., WITH CERTIFICATE OF CONFORMANCE, PACK SLIP NO. 1781911
DATED MAR 18, 2016. PERFORMED OPS CHECK WITH NO DISCREPANCIES. WORK DONE TAW WESTERN
COMMANDER , INC . WIRING DIAGRAM NO. 08030131 - BLEED AIR CONTROL MONITOR, DATED 2/10/89.
Labor USD:
Pans USD:
Billing Method
Hours
Rate
Total
Time and Material
Time and Material
ST
8.14
®
$132.00
$1,074.48
$27.90
Total USD:
$1,102.38
Pans:
Ref. No.
Pan number
Description
Quantity
Sell price USD
Extended USD
6.8#1
NIS3106F12S-35
CONNECTOR
527.90
$27.90
For detail description of the work complied with see the Work Order Detail report.
Westficld_OAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rpt
Page 6 of 14
Printed: 49/2016 4:26:50AM
LS MO
EFTA00597059
Bill To: HYPERION AIR, INC.
WO #: SC13577
Invoice Number: 6916001251
Step: 6.8.1
Completed
REMOVED AND REPLACED CONNECTOR LEFT ENGINE PYLON TEMP
SENSOR P/N MS3106F12S-35 NEW FROM ELECTRO ENTERPRISES INC.,
WITH CERTIFICATE OF CONFORMANCE, PACK SLIP NO. 1781911 DATED
MAR 18, 2016. WORK DONE IAW WESTERN COMMANDER , INC. WIRING
DIAGRAM NO. 08030131 - BLEED AIR CONTROL MONITOR, DATED 2/10189.
Step: 6.8.2
Completed
PERFORMED OPS CHECK IN ACCORDANCE WITH WESTERN COMMANDER,
INC. WIRING DIAGRAM NO. 08030B1 - BLEED AIR CONTROL MONITOR.
DATED 2/10/89.
Discrepancy: 6.9
DURING AIRCRAFT POWER "ON", FOUND DC VOLTS ON ELECTRICAL POWER MONITOR TO READ
8.2 VOLTS WHEN SWITCH IS SET TO "AUX"
Resolution: APPLIED POWER TO AIRCRAFT AND OBSERVED 8.2 VOLTS DC DISPLAYED IN TILE POWER MONITOR
WITH AUX SELECTED. NOTED ALSO THAT IT WOULD ERRATICALLY JUMP FROM Si VOLTS TO 48.2
VOLTS TO 88.2 VOLTS AND BACK TO 8.2 VOLTS. WHEN SELECTING RADIO MASTER TO ON 28 VOLTS IS
DISPLAYED ON THE MONITOR WITH AUX SELECTED. CAN ALSO GET 28 VOLTS TO BE DISPLAYED BY
SELECTING THE PILOT, EICAS, AND COPILOT DISPLAYS TO ON. WHEN SELECTED BACK TO OFF, Si
VOLTS IS DISPLAYED ON TIIE MONITOR AGAIN. CHECKED DC ESS TEST POINT ON PILOT CIRCUIT
BREAKER PANEL AND READ 28 VOLTS WHILE POWER MONITOR STILL READ 8.2 VOLTS. ALL WORK
PERFORMED IN ACCORDANCE WITH GIV WIRING DIAGRAM MANUAL 24-30-00 DC POWER SUPPLY
SYSTEM. CUSTOMER HAS INDICATED TIIAT TIIIS IS A KNOWN ISSUE, AND THAT IT EXISTS IN NO
CONFIGURATION OTHER THAN AUX. CUSTOMER ELECTS NO FURTHER ACTION AT THIS TIME.
Labor USD:
Billing Method
Hours
Rate
Total
Time and Material
ST
7.76
®
5132.00
51,024.32
Total USD:
51,024.32
Step: 6.9.1
Step: 6.9.2
Completed
APPLIED POWER TO AIRCRAFT AND OBSERVED 8.2 VOLTS DC DISPLAYED
IN THE POWER MONITOR WITH AUX SELECTED. NOTED ALSO THAT IT
WOULD ERRATICALLY JUMP FROM 8.2 VOLTS TO 48.2 VOLTS TO 88.2
VOLTS AND BACK TO 8.2 VOLTS. WHEN SELECTING RADIO MASTER TO ON
23 VOLTS IS DISPLAYED ON THE MONITOR WITH AUX SELECTED. CAN
ALSO GET 28 VOLTS TO BE DISPLAYED BY SELECTING THE PILOT, EICAS,
AND COPILOT DISPLAYS TO ON. WHEN SELECTED BACK TO OFF, 8.2
VOLTS IS DISPLAYED ON THE MONITOR AGAIN. AFTER POWER WAS ON
FOR ABOUT AN HOUR THE SAME 8.2 VOLT INDICATION COULD BE SEEN ON
THE POWER MONITOR BUT THIS TIME WITH EITHER AUX OR ESSENTIAL
SELECTED. CHECKED DC ESS TEST POINT ON PILOT CIRCUIT BREAKER
PANEL AND READ 28 VOLTS WHILE POWER MONITOR STILL READ 8.2
VOLTS. ALL WORK PERFORMED IN ACCORDANCE WITH GIV WIRING
DIAGRAM MANUAL 24-30-00 DC POWER SUPPLY SYSTEM.
Completed
GAINED ACCESS TO CONNECTORS 318A1A5P2 AND 318A1A5P3 BY
REMOVING THE COCKPIT ENTRYWAY CENTER HEADLINER.
DISCONNECTED 318A1A5P2 AND BACKPINNED PIN "BB". APPLIED POWER
TO AIRCRAFT. WHILE MONITORING ELECTRICAL POWER MONITOR
PANEL -AUX PWR SW SELECTED, FOUND THAT DC VOLTAGE INDICATION
WOULD FLUCTUATE BETWEEN 8.2, 48.2, AND 88.2 VD( INTERMITTENTLY
WHILE INPUT VOLTAGE AT PINN BB OF CONNECTOR 318A1A5P2 PIN BB
SHOWS STEADY 14.7 VOLTS DC. CONNECTED 318A1A5P2. DISCONNECTED
318A1A5P3 AND BACKPINNED PIN "BB". APPLIED POWER TO AIRCRAFT.
WHILE MONITORING ELECTRICAL POWER MONITOR PANEL WITH ESS
PWR SW SELECTED, AGAIN FOUND THAT DC VOLTAGE INDICATION
WOULD FLUCTUATE BETWEEN 8.2.48.2. AND 88.2 VDC INTERMITTENTLY
WHILE THE INPUT VOLTAGE AT PIN ^BB^ OF CONNECTOR 318A1A5P3
SHOWS A STEADY VOLTAGE READING. SECURED CONNECTOR 318A1A5P3.
SECURED COCKPIT ENTRYWAY CENTER HEADLINER. CONFIRMED BAD
EPMP. WORK WAS DONE WITH REFERENCE TO GIV
24-02-00. DC
ELECTRICAL POWER - ELECTRICAL SCHEMATIC.
Discrepancy: 6.10
PILOTS WIPER MOTOR ONLY OPERATES AT LOW SPEED.
For detail description of the work complied with see the Work Order Detail report.
Westfield GAC Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rpt
Page 7 of 14
Printed: 4(912016 4:26:50AM
LS MO
EFTA00597060
Bill To: HYPERION AIR, INC.
WO #: SCI3577
Invoice Number: 6916001251
Resolution: APPLIED POWER TO AIRCRAFT AND CHECKED FOR PROPER CONTROL VOLTAGE AT PILOT WIPER
CONTROL ASSEMBLY AND FOUND NO HALO VOLTAGE PRESENT. SWAPPED PILOT AND COPILOT WIPER
ON/OFF SWITCHES ON COP AND FOUND DISCREPANCY FOLLOWED SWITCH. RETURNED COPILOT
SWITCH BACK TO ITS ORIGINAL LOCATION. CONFIRMED PILOT WIPER ON/OFF SWITCH (P/N: 4271-503)
IS FAULTY. RECEIVED OK TO INSTALL. RECEIVED AND INSTALLED NEW WIPER ON/OFF SWITCH (P/N:
4271-503) FROM GAC SAVANNAH, REFERENCE 8130-3 DATED 16DEC2015, FORM TRACKING NUMBER:
20151216093100, APPROVAL / AUTHORIZATION NUMBER: ODA-511131-CE, INTO THE PILOT POSITION.
WORK PERFORMED IAA' GIV WDM 30-43-00. REFERENCE GULFSTREAM WESTFIELD WORK ORDER
SC13577.18.15 FOR SYSTEM OPS CHECK.
Billing Method
Hours
Rate
Total
Labor USD:
Time and Material
ST
6.35
@
$132.00
511311.20
Pans USD:
Time and Material
5694.90
Total USD:
$1.53.3.10
Pans:
Ref. No.
Part number:
Description
Quantity
Sell price USD
Extended USD
6.10#1
4271-503
SWITCH LIGHT ASSEMBLY
I
5674.10
$674.10
6.10#2
D436-37
SLEEVE
10
51.42
514.20
6.10#3
D436-38
SLEEVE
4
51.65
$6.60
Step: 6.10.1
Completed
APPLIED POWER TO AIRCRAFT AND CHECKED FOR PROPER CONTROL
VOLTAGE AT PILOT WIPER CONTROL ASSEMBLY AND FOUND NO HULO
VOLTAGE WAS PRESENT. SWAPPED PILOT AND COPILOT WIPER ON/OFF
SWITCHES ON COP AND FOUND DISCREPANCY FOLLOWED SWITCH.
RETURNED SWITCHES BACK TO THERE ORIGINAL LOCATIONS,
CONFIRMED PILOT WIPER ON/OFF SWITCH PIN 4271-503 IS FAULTY.
REFERENCED GIV WDM 30-43-00 FOR WORK PERFORMED.
Discrepancy: 6.11
DURING COCKPIT COMPARTMENT ABOVE FLOOR INSP CMP 532017 NOTED ON CO-PILOTS SIDE
CONSOLE AREA AFT END IS A BROKEN SWITCH LABLED ON/OFF.
Resolution: ACCOMPLISHED MINOR ALTERATION AND REMOVED DISCREPANT SWITCH P/N MTL-206N LABELED
COCKPIT LCD FROM COCKPIT SIDE CONSOLE AND BAGGED AND STOWED CONNECTOR AT SWITCH,
REFERENCE KC AVIATION DWG NO. GIV-31085-31-52. CAPPED AND STOWED WIRE "AS100CC20" AT
AIRSHOW C/B, REFERENCE KC AVIATION DWG NO. GIV-31085-31-52. DISCREPANT SWITCH WAS GIVEN
TO CUSTOMER FOR FURTHER EVALUATION AND REPAIR. INSTALLED A PLUG TO COVER REMAINING
HOLE DUE TO SWITCH REMOVAL. WEIGHT AND BALANCE CHANGE NEGLIGIBLE.
Billing Method
Hours
Rate
Total
Labor USD:
Pans USD:
Time and Material
Time and Material
ST
6.21 @
$132.00
58 19.72
55.16
Total USD:
$824.88
Parts:
Ref. No.
Part number.
Description
Quantity
Sell price USD
Extended USD
6.11 #1
AN525-10-7
SCREW
2
S2.58
$5.16
Item: 7
INTERIOR
For detail description of the work complied with see the Work Order Detail report.
Westficld_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
Orderinvoice.rpt
Page 8 of 14
Printed: 49/2016 4:26:50AM
LS MO
EFTA00597061
Bill To: HYPERION AIR, INC.
WO #: SCI3577
Invoice Number 6916001251
Team Manager:
Charles Heinle
Customer Coordinator:
Vinny Cicala
Part/Model 4:
AC Serial No.fTail No.:
TSN/TSO:
CSN/CSO:
Aircraft Timc:
Discrepancy: 7.1
1 @ PROVIDE DOCUMENTATION OF REMOVED/REINSTALLED INTERIOR COMPONENTS ONLY.
Resolution: THE INTERIOR COMPONENTS REFERENCED IN THE
LOG (RDS 002) HAVE BEEN REMOVED AND
REINSTALLED USING GENERAL SHOP PRACTICES AND EXISTING HARDWARE. ANY COMPONENT
REQUIRING OPERATIONAL OR LEAK CHECK HAS BEEN CHECKED FOR NORMAL OPERATIONS WITH NO
DISCREPANCIES NOTED.
Discrepancy: 7.2
CUSTOMER REPORTS THE COPILOTS AIR VENT IS INOP AND BROKEN.
Resolution: PROVIDED ACCESS TO GASPER. FOUND AIRVENT BROKEN .INSTALLED NEW CUSTOMER SUPPLIED AIR
OUTLET P/N 1747-2. REFERENCE PART AND MATERIAL CERTIFICATION FORM , REFERENCE/SO# 726461
DATED 3/1412016 PERFORMED A OPERATIONAL CHECK OF GASPER . GASPER CHECK IS GOOD. NO
DEFECTS NOTED AT THIS TIME.
REF. R/ D LOG FOR OPERATIONAL CHECK OF GASPER ON APU RUN .
Labor USD:
Pans USD:
Total USD:
Parts:
Ref. No.
Billing Method
Hours
Rate
Total
Time and Material
ST
9.77
(fr,
$132.00
$1,289.64
Time and Material
$1.56
Part number:
Description
41,291.20
Quantity
Sell price USD
Extended USD
7.2#3
MS27039-0814
Step: 7.2.1
Completed
Step: 7.2.2
Completed
SCREW
2
50.78
$1.56
FOUND AIRVENT BROKEN .ORDERED NEW AIR OUTLET P/N 1747-2 NSN ,
RECIEVED AND INSTALLED NEW AIR OUTLET P/N 1747-2. REFERENCE PART
OR MATERIAL CERTIFICATION FORM , REFERENCE/SO/I 726461 DATED
3/14/2016
COPILOTS AIR VENT REQUIRES OPS CHECK DURING A/C RUNS.
Discrepancy: 73
CUSTOMER REPORTS THE CAPTAIN'S AIR-VENT IS BROKEN.
Resolution: PROVIDED ACCESS TO CAPTAINS GASPER. FOUND AIRVENT BROKEN. INSTALLED NEW CUSTOMERS
SUPPLIED GASPER AIR OUTLET P/N 1747-2. REFERENCE PART AND MATERIAL CERTIFICATION FORM ,
REFERENCE/SO# 726461 DATED 3/14/2016. PERFORMED A OPERATIONAL CHECK OF GASPER. GASPER
CHECK IS GOOD . NO DEFECTS NOTED AT THIS TIME.
REF. R/ D LOG FOR OPERATIONAL CHECK OF
GASPER ON APU RUN .
Labor USD:
Billing Method
Hours
Time and Material
ST
Rate
Total
7.93
@
$132.00
$1,046.76
Total USD:
41,046.76
For detail description of the work complied with see the Work Order Detail report.
Westfield_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rpt
Page 9 of 14
Printed: 4/912016 4:26:50AM
LS MO
EFTA00597062
Bill To: HYPERION AIR, INC.
WO #: SCI3577
Invoice Number: 6916001251
Step: 7.3.1
Step: 7.3.2
Completed
Completed
FOUND AIRVENT BROKEN .ORDERED NEW AIR OUTLET PIN 1747-2 NSN ,
RECIEVED AND INSTALLED NEW AIR OUTLET PIN 1747-2. REFERENCE PART
OR MATERIAL CERTIFICATION FORM , REFERENCE/SO# 726461 DATED
3/1412016
PILOTS AIR VENT REQUIRES OPS CHECK DURING A/C RUNS.
Discrepancy: 7.4
CUSTOMER REPORTS THE AIR VENT IN FWD LAV IS INOP.
Resolution: UPON INVESTIGATION FOUND GASPER RETAINING RING LOOSE ON BACK SIDE OF GASPER . SECURED
THE RETAINING RING ON BACKSIDE OF GASPER AS REQUIRED.GASPER IS NOW OPERATIONAL
.PERFORMED A OPERATIONAL CIIECK OF GASPER . GASPER CIIECK IS GOOD. NO DEFECTS NOTED AT
THIS TIME.
REF. R/ D LOG FOR OPERATIONAL CIIECK OF GASPER ON APU RUN .
Billing Method
Hours
Rate
Total
Labor USD:
Time and Material
ST
10.18
@
S132.00
$1,343.76
Total USD:
51,343.76
Step: 7.4.1
Step: 7.4.2
Completed
Completed
I REMOVED GASPER AIR VENT FROM THE FWD LAV PSU.I TIGHTENED THE
GASPER VENT BACKING THEN THEN RE-INSTALLED THE GASPER VENT
INTO THE FWD LAV PSU.THE GASPER NOW OPENS AND CLOSES PROPERLY.
FWD LAV AIR VENT REQUIRES OPS CHECK DURING A/C RUNS.
Discrepancy: 7.5
CUSTOMER REPORTS THE FWD LEFT SIDE WINDOW SHADE IS INOP (MOTOR CHANGE).
Resolution: GAINED ACCESS TO THE VII #1 CABIN WINDOW SIIADE BY REMOVING UN #3 DADO PANEL, UM #2
CUPRAIL SPEAKERS, AND LAI #1 DECO PANEL. REMOVED THE LAI #1 CABIN WINDOW SIIADE P/N
NISA-005-013-19-P-ANN SIN 1535. SENT SHADE ASSEMBLY OUT TO AERO-NASH AVIATION, INC FOR
REPAIRS. RECEIVED REPAIRED SHADE ASSEMBLY FROM AERO-NASA AVIATION INC, REF 8130-3
FT#A-259-0, DATED 3/18/2016. INSTALLED VII WINDOW SHADE P/N MSA-005-013-19-P-ANN SIN 1535.
TURNED A/C POWER ON AND CYCLED THE Lql CABIN WINDOW SHADE MULTIPLE TIME, SHADE OPS
CHECKED GOOD. INSTALLED THE Litt #1 DECO PANEL. VII #2 CUPRAILS SPEAKERS, AND VII #3 DADO
PANEL.
Billing Method
Hours
Rate
Total
Labor USD:
Time and Material
Services USD:
Time and Material
ST
8.67 ®
$132.00
51,144.44
41,776.25
Total USD:
52,920.69
Services:
Ref. No.
Description
7.5 #1
GAC REPAIRS
Part Ref: MSA-005-013-19-P-ANN cabin window shade
Quantity
Sell Price USD
Extended USD
1.00
51,776.25
$1,776.25
Discrepancy: 7.6
CUSTOMER REPORTS THAT TIIE COPILOT'S WINDOW SHADE NEEDS NEW TINT INSTALLED.
*** GULFSTREAM PBI WARRANTY CONSIDERATION
Resolution: RECEIVED CUSTOMERS CO-PILOT WINDOW SHADE, AND HOLDER. REMOVED CUSTOMERS OLD
WINDOW SHADE FROM THE HOLDER. RECEIVED NEW SHADE WITH TINT FROM SOLAR-SCREEN WITH
CERTIFICATE OF CONFORMANCE WITH INVOICE#V1089, DATED SEPTEMBER I, 2003. INSTALLED NEW
WINDOW SHADE TINT ONTO WINDOW SHADE HOLDER. WINDOW SHADE OPS CHECKS OK.
For detail description of the work complied with see the Work Order Detail report.
Westfield_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrdcrInvoice.rpt
Page 10 of 14
Printed: 4(9/2016 4:26:50AM
120
EFTA00597063
Bill To: HYPERION AIR, INC.
WO #: SCI3577
Invoice Number: 6916001251
Discrepancy: 7.7
CUSTOMER REQUEST TO CHECK ALL OVERHEAD LIGHTS AND GLARE SHIELD LIGHTS FOR
PROPER OPERATION (SOME AREAS ARE DARK, BY BOOST PUMPS, AND TRIM WHEEL).
Resolution: CUSTOMER ELECT'S NO ACTION TAKEN AT THIS TIME.
Discrepancy: 7S
CUSTOMER REQUEST TO INSTALL NEW RUBBER SEALS DUE TO WATER LEAK IN REARS GALLON
TANKS.
Resolution: VERIFIED WATER LEAKING FROM #1 AND #2 WATER TANK CAPS, REMOVED LEAKING SEALS FROM #1
AND #2 TANK CAPS AND INSTALLED NEW SEALS, P/N 36082. RECEIVED FROM DYNAMO AVIATION INC.
REFERENCE COC # 16624 DATED FEB-18-2013. FILLED WATER TANKS AND FOUND NO LEAKS FROM CAP
SEALS. WORK PERFORMED IAW GIV GAC DWG SC42716008
REMOVED SIX LEAKING O-RINGS FROM THE QUICK DISCONNECTS ON THREE 5 GALLON WATER
TANKS, INSTALLED SIX NEW O-RINGS P/N 902-9-292 NSN. ON TILE QUICK DISCONNECTS ON THREE S
GALLON WATER TANKS. PARTS RECEIVED FROM SELL GMBH REFERENCE EASA FORM 1 WITH
TRACKING # SP 2012 0080340818 AND W.O #0004151514 DATED 17 OCT 2012. LEAK CHECKED WITH NO
DEFECT'S NOTED. WORK PERFORMED IAW GIV GAC DWG SC42716008.
Labor USD:
Parts USD:
Billing Method
Hours
Rate
Total
Time and Material
Time and Material
ST
2.22
@
$132.00
$293.04
$181.26
Total USD:
$474.30
Parts:
Rcl. No.
Part nutohn:
Description
Quantity
Sell price USD
Extended USD
7.891
36082
ORING
2
$53.50
$107.00
7.8 92
902-9-292
ORING
6
$3.46
$20.76
7.8 93
36082
ORING
I
$53.50
$53.50
Step: 7.8.1
Step: 7.8.2
Completed
VERIFIED WATER LEAKING FROM #1 AND #2 WATER TANK CAPS,
REMOVED LEAKING SEALS FROM #1 AND #2 TANK CAPS AND INSTALLED
NEW SEALS, P/N 36082. RECEIVED FROM DYNAMO AVIATION INC.
REFERENCE COC I/ 16624 DATED FEB-18-2013. FILLED WATER TANKS AND
FOUND NO LEAKS FROM CAP SEALS. WORK PERFORMED IAW GIV GAC
DWG SC42716008
Completed
REMOVED SIX LEAKING O-RINGS FROM THE QUICK DISCONNECTS ON
THREE 5 GALLON WATER TANKS, INSTALLED SIX NEW O-RINGS P/N
902-9-292 NSN. ON THE QUICK DISCONNECTS ON THREE 5 GALLON WATER
TANKS. LEAK CHECKED WITH NO DEFECTS NOTED. WORK PERFORMED
IAW GIV GAC DWG SC42716008.
Discrepancy: 7.9
UPON REMOVAL OF CARPET IN AFT LAVATORY FOUND CARPET WET. SOAKED WITII WHAT
SEEMS TO BE TOILET WATER.
For detail description of the work complied with see the Work Order Detail report.
Westficld_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rot
Page 11 of 14
Printed: 4(9/2016 4:26:50AM
LS MO
EFTA00597064
Bill To: HYPERION AIR, INC.
WO #: SCI3577
Invoice Number 6916001251
Resolution: PERFORMED VISUAL INSPECTION OF AFT LAV TOILET ASSY. NO EVIDENCE OF BLUE STAINING ON
UPPER PORTION OF TANK AROUND LINE CONNECTIONS. DUMPED AFT LAY TANK AND SERVICED WITH
5 GALLONS OF WATER. FLUSHED TOILET A TOTAL OF TWELVE CYCLES WITH NO LEAKS NOTED.
CUSTOMER NOTED THAT THERE IS A IIISTORY OF LINE SVE OVERSERVICING TIIE LAV. RESULTING IN
FLUID ON FLOOR.
NO LEAKAGE NOTED AT THIS TIME.
Billing Method
Hours
Rate
Total
Labor USD:
Time and Material
Services USD:
Time and Material
Total USD:
Services:
Ref. No.
Description
ST
2.40
Ct
$132.00
$316.80
$62.50
7.9 #1
AIRCRAFT CLEANING
Step: 7.9.1
Step: 7.9.2
5379.30
Quantity
Sell Price USD
Extended USD
1.00
562.50
562.50
Completed
PERFORMED VISUAL INSPECTION OF AFT LAY TOILET ASSY. NO EVIDENCE
OF BLUE STAINING ON UPPER PORTION OF TANK AROUND LINE
CONNECTIONS. DUMPED AFT LAV TANK AND SERVICED WITH 5 GALLONS
OF WATER. FLUSHED TOILET A TOTAL OF TWELVE CYCLES WITH NO
LEAKS NOTED.
Completed
ENTERED IN ERROR.
Item: 10
ADMINISTRATIVE USE FOR FUEL ONLY, NO RETURN TO SERVICE REQUIRED
Team Manager:
Charles Heiwig
Customer Coordinator:
Vinny Cicala
Partfivlodel #:
AC Serial No./Tail No.:
TSN/TSO:
CSN/CSO:
Aircraft Time:
Discrepancy: 10.1
ADMINISTRATIVE USE ONLY TO FUEL AND DEFUEL AIRCRAFT AS REQUIRED
Resolution: BILLING OF FUEL FOR AIRCRAFT AS REQUIRED.
Billing Method
Hours
Rate
Total
Pans USD:
Time and Material
54,292.00
Total USD:
54,292.00
Parts:
Ref. No.
Pan number.
Description
Quantity
Sell price USD
Extended USD
10.1 MI
JET-A
FUEL, AVIATION TURBINE
1,073
54.00
54,292.00
Item: 11
NZ2010 V6.1 FMS SYSTEM UPGRADE - TRIPLE
Team Manager:
Charles Heiwig
Customer Coordinator:
Ninny Cicala
Pan/Model #:
AC Serial No./Tail No.:
TSN/TSO:
CSN/CSO:
Aircraft Time:
For detail description of the work complied with see the Work Order Detail report.
Westfield_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rpt
Page 12 of 14
Printed: 4/9/2016 4:26:50AM
LS MO
EFTA00597065
Bill To: HYPERION AIR, INC.
WO #: SCI3577
Discrepancy: 11.1
ASC 477A NZ2010 V6.I FMS SYSTEM UPGRADE - TRIPLE
Invoice Number 6916001251
THIS AIRCRAFT SERVICE CHANGE UPGRADES THE EXISTING NZ-2000 FLIGHT MANAGEMENT
SYSTEMS (FMS), VIA INSTALLATION OF VERSION 6.1 SOFTWARE, TO AN NZ-2010 SYSTEM WITH
SBAS/LPV GPS UPGRADE.
NEW COMPONENTS:
TWO (2) HONEYWELL WAAS CAPABLE GPS RECEIVERS (PART NUMBER (PN) HG202IKB01)
TWO (2) WAAS CAPABLE GPS ANTENNAS (PN S67-1575-137)
ONE (1) ASC 477 KIT, NZ-2000 FLIGHT MANAGEMENT SYSTEM (FMS) 6.1 UPGRADE.
MODIFIED COMPONENTS:
THREE (3) EACH HONEYWELL NZ-2000 NAVIGATION COMPUTERS (PN 7018879-030XX TO
7018879-03036)
TWO (2) EACH HONEYWELL PZ-800 PERFORMANCE COMPUTERS (PN 7004609-XXX TO 7004609-940)
PERFORMANCE COMPUTERS NOT AT A MINIMUM LEVEL OF PN 7004609-925 WILL REQUIRE
ADDITIONAL UPGRADES NOT COVERED BY THIS INSTALLATION. ADDITIONAL CHARGES WILL
APPLY.
PREREQUISITES:
NZ-2000 COMPUTERS: HARDWARE MOD "E". FOR UNITS WITHOUT THIS MODIFICATION,
HONEYWELL SERVICE BULLETIN 7018879-34-0051 (PUB. NO. A21-6111-004) WILL BE REQUIRED.
ESTIMATED ADDITIONAL COST IS $2,600/UNIT.
PZ-800 COMPUTERS: PART NUMBER 7004609-925. FOR UNITS NOT AT THE -925 LEVEL OR
HIGHER, ADDITIONAL MODIFICATIONS ARE REQUIRED AND WILL BE ADDRESSED ON A TIME
AND MATERIAL BASIS.
THE AIRCRAFT MUST CURRENTLY BE EQUIPPED WITII DUAL GLOBAL POSITIONING SYSTEM
(GPS) RECEIVERS.
H AIRCRAFT SERIAL NUMBERS 1000 THROUGH 1389: GPS #1 AND #2 INSTALLATIONS NOT
INSTALLED BY GULFSTREAM STC ST01716AT-D WILL REQUIRE ENGINEERING REVIEW PRIOR TO
INCORPORATION OF TIIIS ASC.
1 EXISTING FMS #1 AND #2 INSTALLATIONS MUST MATCH GULFSTREAM STC ST01715AT-D OR
EQUIVALENT PRIOR TO INCORPORATION.
CONCURRENT REQUIREMENTS: NONE
RE: PROPOSAL# 7024273 R0I (GAC1015-2422-GIV-1085-R01)-1.1
Resolution: CUSTOMER ELECTS NO ACTION THIS IS ADMINSTRATIVE ONLY TO CAPTURE INVOICEING OF PARTS.
Billing Method
Hours
Rate
Total
Labor USD:
Time and Material
ST
25.00
®
$132.00
$3,300.00
Pans USD:
Time and Material
$35.00
Services USD:
Time and Material
$2,640.00
Total USD:
55,975.00
Pans:
Ref. No.
Part number:
Description
Quantity
Sell price USD
Extended USD
11.1 #9
AIRCRAFT-HISTORY
FAA AIRCRAFT HISTORY RECORDS
I
$35.00
$35.00
Services:
Ref. No.
Description
Quantity
Sell Price USD
Extended USD
11.1 #1
GAC REPAIRS
1.00
$1,320.00
$1,320.00
11.1 #2
GAC REPAIRS
1.00
$1,320.00
$1,320.00
For detail description of the work complied with see the Work Order Detail report.
Westfield_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rpt
Page 13 of 14
Printed: 4(9/2016 4:26:50AM
LS MO
EFTA00597066
Bill To: HYPERION AIR, INC.
WO #: SC13577
Invoice Number: 6916001251
Communications concerning disputed debts, including a check or other instrument
tendered as full satisfaction of a debt, must be forwarded to:
Gulfstream Aerospace
Ann. Credit Manager
PO Box 2206
M/S B-05
Savannah, GA 31402
For detail description of the work complied with see the Work Order Detail report.
Westfield_GAC_Work
Unless otherwise indicated, all financial values listed in this document am in US Dollars (USD).
OrderInvoice.rpt
Page 14 of 14
Printed: 49/2016 4:26:50AM
LS MO
EFTA00597067
Document Preview
PDF source document
This document was extracted from a PDF. No image preview is available. The OCR text is shown on the left.
This document was extracted from a PDF. No image preview is available. The OCR text is shown on the left.
Extracted Information
Dates
Document Details
| Filename | EFTA00597054.pdf |
| File Size | 1035.8 KB |
| OCR Confidence | 85.0% |
| Has Readable Text | Yes |
| Text Length | 38,184 characters |
| Indexed | 2026-02-11T22:55:46.710842 |